2017 LongPac Report
It’s Monday afternoon and I just got home and finished unpacking from the race. Even after writing in my log, it is all a bit of a blur but writing helps.
This was my first LongPac and a lot of other firsts along with it. Hopefully it will all fill in.
I camped out in SF the night before, arriving after the fireworks, and managing to get a good rest. Exciter and nervous I stowed the outboard below and mounted the e-rudder cassette. 09:30 I pushed off and sailed out for my 10:00 start. Checked in with the race committee and crossed the line on port in good order carrying main and #3 jib. Headed for the north tower to work my way out from that side but tacked early to avoid an inbound freighter. South side it is. Other boats opted for more sail and it was paying off. After getting past the lightship I changed up to my 125% which is my #1 and carried it until just before dark. I did manage to get my first nap down below on the port bunk. Things are definitely LOUDER below, with the hull slamming over the waves the reverberations were astonishing. It would rouse me regularly so I could pop my head out for a look around and check AIS.
Seasickness wasn’t too bad but had me pretty lethargic. My first check in Wed. night, trying to text on the Delorme was pretty brutal though. Barely got a very short text off to R/C and home. Maintaining a regime of Dramamine helps.
Changed down to the #3 jib and put a few more layers on as night came and it got cooler. The moon made things beautiful. First night proceeded as the day with regular naps and and lookouts, keeping an eye on AIS. After the moon went down I saw the phosphorecence in the bow wave, absolutely amazing!
Thursday morning brought a new set of issues, the solar system wasn’t charging. After checking in I tried resetting the charge controller through the app in my phone, but trying to focus on that really brought on the seasickness. After a rest I decided I needed to get into the wiring. We hove to for some relief from the swell and dug out the tools and multimeter. After some periods of rest, work, purge, the problem was solved. Aimed west again I went below, dosed up on dramamine and took a nap. Evening check in completed, kept getting a little more food and fluids in me.
About 50nm from turn around I heard Kyntanna on the radio. I called to say hello, and started to chat. Got scolded by USCG Station Long Beach. Oops. at 02:56 Friday I made my turn. Woo hoo!!
Friday things continued to improve as far as seasickness, appetite, and energy level. Communications became easier. Running with the swell helps a lot for me.
Wind began to increase throughout the day with the first reef in midday and apparent wind passing 18 knots, later I tucked in the second after we were hitting 22 plus.
Around 19:00 the tillerpilot ram gave up. Something inside, I‘ll have to take it apart to see if I can fix it. I have and ST2000 for a backup but it couldn’t keep up with the swell and wind waves that were building. With check in I alerted R/C and home I would heave to later for rest. 22:00 I did just that, dozed for a couple hours when a big wave slammed the side and startled me, all was ok so I tried for a little more sleep. Saturday 02:00 I set to getting to the finish, hand steering in that cross sea the last 100 miles.
I tried the backup pilot a couple times when I just couldn’t keep my eyes open but only got a very short nap. As the sun came up it became easier to keep alert. 08:00 check in had me just west of the Farallone Islands with a thick haze keeping them obscured until I was within 2.5 miles. I considered the lee shore for a moment but felt ok passing to the north in the conditions at hand.
Approaching Point Bonita I was pleased to receive Red Sky’s welcome back call on the radio. The wind died and I jibed back and forth to keep apparent wind going, keep us in the flood and between the inbound and outbound shipping traffic, up to the Gate, where the breeze filled in, put us on starboard to the finish. I ran all the way to the breakwater to give R/C a big wave and THANK YOU! Altogether a great race, challenging and exciting!
Sailed back to Richmond, called my wife on the way, and slept hard. Ate and slept some more. Cleaned and stowed the boat on Sunday. Returned the liferaft and headed home on Monday. Whew!
I’m sure there is plenty I’ve missed, hopefully this will suffice.
Oh, I didn’t mention the groover, or bucket and chuck it, as I’ve heard it called.
That was a first under a seaway. We’ll skip the details.
Greg Ashby
S/V Nightmare